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Post by Matthew on Mar 27, 2019 10:13:10 GMT
Hi, I have got my eChook all set up and all the features work well apart from the MotorPWM output. Currently when I press the throttle button: - Pin D5 on the Arduino goes to 5V
- The PWM LED turns on
- The MotorPWM output on goes to 2.67V
Additionally, on releasing the accelerator button it takes about one second for the arduino output to respond.
Can you suggest any solution, or do you have a circuit diagram for the board so I can do more fault finding.
Thanks
Matt
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Post by Rowan on Mar 27, 2019 11:34:36 GMT
Hi Matt, Glad it's mostly working... The circuit schematic is here: docs.eChook.uk/circuit-schematics/pwm-outputFirst things to check are the resistor values, then the voltages at the components, if no issues are found I'll have another think! The delay on the throttle backing off is odd, have you modified the Arduino code at all? I'd set debug to true in the code then add a serial print every time it reads the throttle and updates the pwm, then you can watch it through the serial and get more of an idea what's happening. Edit: is the output from the board connected to anything when you measure 2.7v?
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Post by sammi on Nov 21, 2019 11:58:10 GMT
hi, I am trying to solder the hall effect sensor to the project but can not figure out which leg is which, how do I identify this?
thanks sammi
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Post by Rowan on Nov 21, 2019 12:37:41 GMT
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Post by sammi on Dec 3, 2019 13:00:10 GMT
Hi Rowan,
Thank you that contained all the information I was looking for
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